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Report No.
 - 

Overheating failure analysis of steam generator tubes II; Overheating failure analysis of U.K.PFR superheater

Hamada, Hirotsugu  ; Tanabe, Hiromi

If a sodium-water reaction jet was formed due to water leakage in an FBR steam generator(SG), neighboring tubes would suffer from overheating. On the safety aspect of the SGs, it is important to confirm that the neighboring tubes would not fail under such a severe overheating condition. So far, an analytical model using the structural integrity analysis code, FINAS, has been prepared and validated by the explosive torch overheating test data. This report presents the results on the overheating failure analysis of the under-sodium leak in the PFR superheater(SH), 1987. In the SH with slow steam dump system in 1987, neighboring overheated tubes are failed about 3 seconds after the SH isolation, which is shown both by the leak in the PFR and its analysis. For the SH in which a fast steam dump system was installed after the leak of 1987, the analysis shows no tube failure due to the fast steam depression and cooling effect inside. These results indicate that the FINAS model adequately predicts the overheating failure and the specific SH design and operation possibly result in further growth of the leak. It is concluded that steam blow effect is extremely important and the analysis model presented here is useful for the overheating failure evaluation of the SGs.

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