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Aso, Tomokazu; Tatsumoto, Hideki*; Otsu, Kiichi*; Kawakami, Yoshihiko*; Komori, Shinji*; Muto, Hideki*; Takada, Hiroshi
JAEA-Technology 2019-013, 77 Pages, 2019/09
At Materials and Life Science experimental Facility (MLF) of the Japan Proton Accelerator Research Complex (J-PARC), a 1-MW pulsed spallation neutron source is equipped with a cryogenic hydrogen system which circulates liquid hydrogen (20 K and 1.5 MPa) to convert high energy neutrons generated at a mercury target to cold neutrons at three moderators with removing nuclear heat of 3.8 kW deposited there. The cryogenic system includes an accumulator with a bellows structure in order to absorb pressure fluctuations generated by the nuclear heat deposition in the system. Welded inner bellows of the first accumulator was failured during operation, forcing us to improve the accumulator to have sufficient pressure resistance and longer life-time. We have developed elemental technologies for manufacturing welded bellows of the accumulator by a thick plate with high pressure resistance, succeeding to find optimum welding conditions. We fabricated a prototype bellows block and carried out an endurance test by adding a pressure change of 2 MPa repeatedly. As a result, the prototype bellows was successfully in use exceeding the design life of 10,000 times. Since distortions given during welding and assembling affect functionality and lifetime of the bellows, we set the levelness of each element of the bellows as within 0.1. The improved accumulator has already been in operation for about 25,000 hours as of January 2019, resulting that the number of strokes reached to 16,000. In July 2018, we demonstrated that the accumulator could suppress the pressure fluctuation generated by the 932 kW beam injection as designed. As current operational beam power is 500 kW, the current cryogenic hydrogen system could be applicable for stable operation at higher power in the future.
Aso, Tomokazu; Teshigawara, Makoto; Hasegawa, Shoichi; Muto, Hideki; Aoyagi, Katsuhiro; Nomura, Kazutaka; Takada, Hiroshi
Journal of Physics; Conference Series, 1021(1), p.012085_1 - 012085_4, 2018/06
Times Cited Count:0 Percentile:0.00(Nuclear Science & Technology)Aso, Tomokazu; Teshigawara, Makoto; Hasegawa, Shoichi; Aoyagi, Katsuhiro*; Muto, Hideki*; Nomura, Kazutaka*; Takada, Hiroshi; Ikeda, Yujiro
JAEA-Technology 2017-021, 75 Pages, 2017/08
Liquid hydrogen is employed as a cold neutron moderator material at the spallation neutron source of Materials and Life science experimental Facility of Japan Proton Accelerator Research Complex (J-PARC). From January 2015, it became observable that the differential pressure between heat exchangers and an 80 K adsorber (ADS) in a helium refrigerator system increased with operating time. In November 2015, the differential pressure rise became more significant, leading to degrade the refrigerating performance in cooling liquid hydrogen. In order to investigate the cause of the abnormal differential pressure rise between the heat exchangers and the ADS, we carried out visual inspection inside the heat exchangers and analyzed the impurities contained in the helium gas. Unfortunately, we could not identify the impurities causing the performance degradation, but observed a trace of oil in the inlet piping of the heat exchanger. Based on investigations of the abnormal events occurred in the refrigerators with similar refrigerating capacity at other facilities, we took measures that cleaning the heat exchangers with Freon and replacing the ADS with new one. As a result, the differential pressure rise phenomenon was removed to recover the performance. We have detected oil from the Freon used for cleaning the heat exchangers and at a felt supporting charcoal packed in the ADS. In particular, oil was accumulated in membranous form onto the felt at the entrance side in the ADS. The amount of oil contained in the helium gas was about 10 ppb or so, less than the design value, in the helium refrigerator. However, the oil accumulated onto the felt in the ADS through long operating period may cause abnormal differential pressure rise, leading to the performance degradation of the helium refrigerator. Further study is needed to specify the cause more clearly.
Tatsumoto, Hideki; Aso, Tomokazu; Otsu, Kiichi; Kawakami, Yoshihiko; Aoyagi, Katsuhiro; Muto, Hideki
IOP Conference Series; Materials Science and Engineering, 101, p.012107_1 - 012107_8, 2015/12
Times Cited Count:2 Percentile:63.46(Thermodynamics)The Japan Proton Accelerator Research Complex (J-PARC) cryogenic hydrogen system was completed in April 2008. The proton beam power was gradually increased to 500 kW. A trial 600-kW proton beam operation was successfully completed in April 2015. We achieved long-lasting operation for more than three months. However, thus far, we encountered several problems such as unstable operation of the helium refrigerator because of some impurities, failure of a welded bellows of an accumulator, and hydrogen pump issues. Furthermore, the Great East Japan Earthquake was experienced during the cryogenic hydrogen system operation in March 2011. In this study, we describe the operation characteristics and our experiences with the J-PARC cryogenic hydrogen system.
Oshima, Katsumi*; Honda, Atsushi; Okano, Fuminori; Usui, Katsutomi; Noto, Katsuya*; Muto, Hideki*; Kawai, Mikito; Oga, Tokumichi; Ikeda, Yoshitaka
Heisei-16-Nendo Osaka Daigaku Sogo Gijutsu Kenkyukai Hokokushu (CD-ROM), 4 Pages, 2005/03
no abstracts in English
Aso, Tomokazu; Teshigawara, Makoto; Hasegawa, Shoichi; Muto, Hideki*; Aoyagi, Katsuhiro*; Takada, Hiroshi; Ikeda, Yujiro
no journal, ,
no abstracts in English
Aso, Tomokazu; Teshigawara, Makoto; Hasegawa, Shoichi; Muto, Hideki*; Aoyagi, Katsuhiro*; Takada, Hiroshi; Ikeda, Yujiro
no journal, ,
no abstracts in English
Teshigawara, Makoto; Aso, Tomokazu; Hasegawa, Shoichi; Muto, Hideki*; Aoyagi, Katsuhiro*; Takada, Hiroshi; Ikeda, Yujiro
no journal, ,
Performance degradation of helium refrigerator was occurred for liquid hydrogen circulation system of J-PARC high intensity neutron source since 2015. In order to find the cause of performance degradation of helium refrigerator, we investigated the impurities in helium gas and accumulated oil in inside cold box components by quadrupole mass spectrometer and organic solvent extraction. The measured impurities and accumulated oil were less than design value. We collected 143g of total amount of accumulated oil from heat exchanger and adosorber, which was corresponded to estimated value from 10 ppb of oil contamination in helium and accumulated operation period. However, we only could find out that accumulated oil like coating film on top surface of felt, which was used to hold the active charcoal in adsorber. We report detailed measurement results of impurities, accumulated oil, etc., to find the cause of performance degradation.
Teshigawara, Makoto; Aso, Tomokazu; Muto, Hideki*; Aoyagi, Katsuhiro*; Takada, Hiroshi; Ikeda, Yujiro
no journal, ,
Performance degradation of helium refrigerator was occurred for liquid hydrogen circulation system of J-PARC high intensity neutron source since 2015. During cause investigation of performance degradation of helium refrigerator, we found out that accumulated oil like coating film on top surface of felt, which was used to hold the active charcoal in adsorber, might cause pressure difference in adsorber. We performed cold nitrogen gas flow test in the felt accumulated oil and found out that frozen oil under cold nitrogen flow caused the pressure difference.
Aso, Tomokazu; Teshigawara, Makoto; Hasegawa, Shoichi; Muto, Hideki*; Aoyagi, Katsuhiro*; Takada, Hiroshi
no journal, ,
Aso, Tomokazu; Teshigawara, Makoto; Muto, Hideki*; Aoyagi, Katsuhiro*; Takada, Hiroshi
no journal, ,
Liquid hydrogen (20 K, 1.4 MPaG) is employed as a cold neutron moderator material at the 1 MW spallation neutron source of Japan Proton Accelerator Research Complex (J-PARC). The cryogenic hydrogen system, combined with a helium refrigerator, was adopted to generate a liquid hydrogen circulation flow (185 g/s). Since January 2015, a pressure drop gradually increased between heat exchangers HXs) and an adsorber (ADS) in the helium refrigerator for each operation, causing the refrigerator performance degradation. The performance of helium refrigerator could be recovered as a result of countermeasures focused on accumulated oil removal, such as cleaning the inside HXs and exchanging the ADS at 2016 summer shutdown, however the detailed cause is still in doubt. On the other hand, a long run stable operation could be secured over 175 days in 2018. Just end of long run operation, a first high-intensity-beam injection with 1MW beam power was also carried out for one hour aiming to confirm the refrigerator performance according to design requirement.
Aso, Tomokazu; Tatsumoto, Hideki; Otsu, Kiichi; Kawakami, Yoshihiko; Komori, Shinji; Muto, Hideki; Takada, Hiroshi
no journal, ,
no abstracts in English
Aso, Tomokazu; Teshigawara, Makoto; Hasegawa, Shoichi; Muto, Hideki; Aoyagi, Katsuhiro; Nomura, Kazutaka; Takada, Hiroshi
no journal, ,
no abstracts in English
Aso, Tomokazu; Teshigawara, Makoto; Hasegawa, Shoichi; Muto, Hideki; Aoyagi, Katsuhiro; Nomura, Kazutaka; Takada, Hiroshi
no journal, ,
no abstracts in English