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JAEA Reports

Data report of ROSA/LSTF experiment TR-LF-15; Accident management actions during station blackout transient with pump seal LOCA

Takeda, Takeshi

JAEA-Data/Code 2023-012, 75 Pages, 2023/10

JAEA-Data-Code-2023-012.pdf:4.45MB

An experiment denoted as TR-LF-15 was conducted on June 11, 2014 using the Large Scale Test Facility (LSTF) in the Rig of Safety Assessment-V (ROSA-V) Program. The ROSA/LSTF experiment TR-LF-15 simulated accident management (AM) actions during a station blackout transient with TMLB' scenario with pump seal loss-of-coolant accident (LOCA) in a pressurized water reactor (PWR). This scenario is featured by loss of auxiliary feedwater functions. The pump seal LOCA was simulated by a 0.1% cold leg break. The test assumptions included total failure of both high pressure injection system and low pressure injection system of emergency core cooling system (ECCS). Also, it was presumed non-condensable gas (nitrogen gas) inflow to the primary system from accumulator (ACC) tanks of ECCS. When steam generator (SG) secondary-side collapsed liquid level dropped to a certain low liquid level, the primary pressure turned to rise. After the SG secondary-side became voided, the safety valve of a pressurizer cyclically opened which led to loss of primary coolant. Core uncovery thus took place owing to core boil-off at high pressure. When an increase of 10 K was confirmed in cladding surface temperature of simulated fuel rods, SG secondary-side depressurization was started as the first AM action. At that time, the safety valves in both SGs were fully opened. Primary depressurization was initiated by completely opening the pressurizer safety valve as the second AM action with some delay after the first AM action onset. When the SG secondary-side pressure lowered to 1.0 MPa following the first AM action, water was injected into the secondary-side of both SGs via feedwater lines with low-head pumps as the third AM action. A reduction in the primary pressure was accelerated because the heat removal from the SG secondary-side system resumed shortly after the third AM action initiation.

JAEA Reports

Data report of ROSA/LSTF experiment IB-HL-01; 17% hot leg intermediate break LOCA with totally-failed high pressure injection system

Takeda, Takeshi

JAEA-Data/Code 2023-007, 72 Pages, 2023/07

JAEA-Data-Code-2023-007.pdf:3.24MB

An experiment denoted as IB-HL-01 was conducted on November 19, 2009 using the Large Scale Test Facility (LSTF) in the Rig of Safety Assessment-V (ROSA-V) Program. The ROSA/LSTF experiment IB-HL-01 simulated a 17% hot leg intermediate break loss-of-coolant accident due to a double-ended guillotine break of pressurizer surge line in a pressurized water reactor (PWR). The break was simulated by a long nozzle upwardly mounted flush with a hot leg inner surface. The test assumptions included total failure of both high pressure injection system of emergency core cooling system (ECCS) and auxiliary feedwater system. In the experiment, relatively large size of break led to a fast transient of phenomena. The primary pressure steeply dropped after the break, and became lower than steam generator (SG) secondary-side pressure. Break flow turned from single-phase flow to two-phase flow soon after the break. Core uncovery started simultaneously with liquid level drop in downflow-side of crossover leg before loop seal clearing (LSC). The LSC was induced in both loops by steam condensation on accumulator (ACC) coolant of ECCS injected into cold legs. The whole core was quenched owing to the rapid recovery in the core liquid level after the LSC. Peak cladding temperature of simulated fuel rods was detected almost concurrently with the LSC. During the ACC coolant injection, liquid levels recovered in the hot legs and SG inlet plena because of liquid entrainment from the hot leg into the SG inlet plenum by high-velocity steam flow. After the continuous core cooling was confirmed through the actuation of low pressure injection system of ECCS, the experiment was terminated. This report summarizes the test procedures, conditions, and major observations in the ROSA/LSTF experiment IB-HL-01.

JAEA Reports

Data report of ROSA/LSTF experiment SB-PV-09; 1.9% pressure vessel top small break LOCA with SG depressurization and gas inflow

Takeda, Takeshi

JAEA-Data/Code 2021-006, 61 Pages, 2021/04

JAEA-Data-Code-2021-006.pdf:2.78MB

An experiment denoted as SB-PV-09 was conducted on November 17, 2005 using the Large Scale Test Facility (LSTF) in the Rig of Safety Assessment-V (ROSA-V) Program. The ROSA/LSTF experiment SB-PV-09 simulated a 1.9% pressure vessel top small-break loss-of-coolant accident in a pressurized water reactor (PWR). The test assumptions included total failure of high pressure injection system and non-condensable gas (nitrogen gas) inflow to the primary system from accumulator (ACC) tanks of emergency core cooling system (ECCS). In the experiment, liquid level in the upper-head was found to control break flow rate. When maximum core exit temperature reached 623 K, steam generator (SG) secondary-side depressurization was initiated by fully opening the relief valves in both SGs as an accident management (AM) action. The AM action, however, was ineffective on the primary depressurization until the SG secondary-side pressure decreased to the primary pressure. Meanwhile, the core power was automatically reduced when maximum cladding surface temperature of simulated fuel rods exceeded the pre-determined value of 958 K to protect the LSTF core due to late and slow response of core exit temperature. After the automatic core power reduction, loop seal clearing (LSC) was induced in both loops by steam condensation on the ACC coolant injected into cold legs. The whole core was quenched because of core recovery after the LSC. After the ACC tanks started to discharge nitrogen gas, the pressure difference between the primary and SG secondary sides became larger. After the continuous core cooling was confirmed through the actuation of low pressure injection system of ECCS, the experiment was terminated. This report summarizes the test procedures, conditions, and major observations in the ROSA/LSTF experiment SB-PV-09.

JAEA Reports

Data report of ROSA/LSTF experiment SB-SL-01; Main steam line break accident

Takeda, Takeshi

JAEA-Data/Code 2020-019, 58 Pages, 2021/01

JAEA-Data-Code-2020-019.pdf:3.85MB

An experiment denoted as SB-SL-01 was conducted on March 27, 1990 using the Large Scale Test Facility (LSTF) in the Rig of Safety Assessment-IV (ROSA-IV) Program. The ROSA/LSTF experiment SB-SL-01 simulated a main steam line break (MSLB) accident in a pressurized water reactor (PWR). The test assumptions were made such as auxiliary feedwater (AFW) injection into secondary-side of both steam generators (SGs) and coolant injection from high pressure injection (HPI) system of emergency core cooling system into cold legs in both loops. The MSLB led to a fast depressurization of broken SG, which caused a decrease in the broken SG secondary-side wide-range liquid level. The broken SG secondary-side wide-range liquid level recovered because of the AFW injection into the broken SG secondary-side. The primary pressure temporarily decreased a little just after the MSLB, and increased up to 16.1 MPa following the closure of the SG main steam isolation valves. Coolant was manually injected from the HPI system into cold legs in both loops a few minutes after the primary pressure reduced to below 10 MPa. The primary pressure raised due to the HPI coolant injection, but was kept at less than 16.2 MPa by fully opening a power-operated relief valve of pressurizer. The core was filled with subcooled liquid through the experiment. Thermal stratification was seen in intact loop cold leg during the HPI coolant injection owing to the flow stagnation. On the other hand, significant natural circulation prevailed in broken loop. When the continuous core cooling was ensured by the successive coolant injection from the HPI system, the experiment was terminated. The experimental data obtained would be useful to consider recovery actions and procedures in the multiple fault accident with the MSLB of PWR. This report summarizes the test procedures, conditions, and major observations in the ROSA/LSTF experiment SB-SL-01.

Journal Articles

Major outcomes through recent ROSA/LSTF experiments and future plans

Takeda, Takeshi; Wada, Yuki; Shibamoto, Yasuteru

World Journal of Nuclear Science and Technology, 11(1), p.17 - 42, 2021/01

Journal Articles

The Working group on the analysis and management of accidents (WGAMA); A Historical review of major contributions

Herranz, L. E.*; Jacquemain, D.*; Nitheanandan, T.*; Sandberg, N.*; Barr$'e$, F.*; Bechta, S.*; Choi, K.-Y.*; D'Auria, F.*; Lee, R.*; Nakamura, Hideo

Progress in Nuclear Energy, 127, p.103432_1 - 103432_14, 2020/09

 Times Cited Count:4 Percentile:20.53(Nuclear Science & Technology)

Journal Articles

Numerical simulation of natural circulation experiment under asymmetric cooldown using LSTF

Ishigaki, Masahiro; Watanabe, Tadashi*

Proceedings of 12th International Topical Meeting on Nuclear Reactor Thermal-Hydraulics, Operation and Safety (NUTHOS-12) (USB Flash Drive), 10 Pages, 2018/10

When coolant in one of the secondary side of steam generator (SG) is lost under some accident condition, the NC in the loop with the affected SG may terminate. Hence, the experiment was done in order to discuss the behavior of the natural circulation flow when the secondary side of the intact SG was depressurized stepwisely and that of the affected SG was empty of coolant. In this paper, we analyzed this NC experiment using the LSTF by the TRACE code. The objective of this analysis is to clarify the sensitivity of the code to the NC behavior. The calculated mass flow rate in the intact loop was slightly underestimated compared with the experimental result. On the other hand, the calculated mass flow rate in the affected loop was overestimated compared with the experimental result. In addition, we did the sensitivity analysis of the NC behavior in the case that the cooldown rate was changed.

Journal Articles

Analyses of LSTF experiment and PWR plant for 5% cold-leg break loss of coolant accident

Watanabe, Tadashi*; Ishigaki, Masahiro*; Katsuyama, Jinya

Proceedings of 12th International Topical Meeting on Nuclear Reactor Thermal-Hydraulics, Operation and Safety (NUTHOS-12) (USB Flash Drive), 9 Pages, 2018/10

The analyses of LSTF experiment and PWR plant for 5% cold-leg break LOCA are performed using the RELAP5/MOD3.3 code. The discharge coefficient of critical flow model is determined so as to obtain the agreement of pressure transient between the LSTF experiment and the experimental analysis, and used for the PWR analysis. The characteristics of thermal-hydraulic phenomena in the experiment are shown to be simulated well by the two analyses. The decrease in core differential pressure during the loop-seal clearing is, however, underestimated by the two analyses, and the core heat up is not predicted. The loop flow rates are also underestimated by the two analyses. Although the duration of core heat up during the boil-off period is longer in the experimental analysis, the results of two analyses agree well, and the effect of scaling is found to be small between the experimental analysis and the PWR analysis.

Journal Articles

ROSA/LSTF test on nitrogen gas behavior during reflux condensation in PWR and RELAP5 code analyses

Takeda, Takeshi; Otsu, Iwao

Mechanical Engineering Journal (Internet), 5(4), p.18-00077_1 - 18-00077_14, 2018/08

JAEA Reports

Data report of ROSA/LSTF experiment SB-SG-10; Recovery actions from multiple steam generator tube rupture accident

Takeda, Takeshi

JAEA-Data/Code 2018-004, 64 Pages, 2018/03

JAEA-Data-Code-2018-004.pdf:3.33MB

Experiment SB-SG-10 was conducted on November 17, 1992 using LSTF. Experiment simulated recovery actions from multiple steam generator (SG) tube rupture accident in PWR. Primary pressure was kept higher than broken SG secondary-side pressure due to coolant injection from high pressure injection (HPI) system into cold and hot legs even after start of full opening of intact SG relief valve (RV). Full opening of power-operated relief valve (PORV) in pressurizer (PZR) resulted in pressure equalization between primary and broken SG systems as well as PZR liquid level recovery. Broken SG RV opened once after start of intact SG RV full opening. Core was filled with saturated or subcooled liquid through experiment. Significant natural circulation prevailed in intact loop after start of intact SG RV full opening. Significant thermal stratification appeared in hot legs especially during time period of HPI coolant injection into hot legs.

JAEA Reports

Data report of ROSA/LSTF experiment SB-PV-07; 1% Pressure vessel top break LOCA with accident management actions and gas inflow

Takeda, Takeshi

JAEA-Data/Code 2018-003, 60 Pages, 2018/03

JAEA-Data-Code-2018-003.pdf:3.68MB

Experiment SB-PV-07 was conducted on June 9, 2005 using LSTF. Experiment simulated 1% pressure vessel top small-break LOCA in PWR under total failure of HPI system and nitrogen gas inflow to primary system from ACC tanks. Liquid level in upper-head was found to control break flow rate. Coolant was started to manually inject from HPI system into cold legs as first accident management (AM) action when maximum core exit temperature reached 623 K. Fuel rod surface temperature largely increased because of late and slow response of core exit temperature. SG secondary-side depressurization was initiated by fully opening relief valves as second AM action when primary pressure decreased to 4 MPa. However, second AM action was not effective on primary depressurization until SG secondary-side pressure decreased to primary pressure. Pressure difference became larger between primary and SG secondary sides after ACC tanks started to discharge nitrogen gas.

Journal Articles

ROSA/LSTF tests and posttest analyses by RELAP5 code for accident management measures during PWR station blackout transient with loss of primary coolant and gas inflow

Takeda, Takeshi; Otsu, Iwao

Science and Technology of Nuclear Installations, 2018, p.7635878_1 - 7635878_19, 2018/00

 Times Cited Count:2 Percentile:20.55(Nuclear Science & Technology)

Journal Articles

RELAP5 uncertainty evaluation using ROSA/LSTF test data on PWR 17% cold leg intermediate-break LOCA with single-failure ECCS

Takeda, Takeshi; Otsu, Iwao

Annals of Nuclear Energy, 109, p.9 - 21, 2017/11

 Times Cited Count:8 Percentile:60.68(Nuclear Science & Technology)

Journal Articles

ROSA/LSTF test and RELAP5 analyses on PWR cold leg small-break LOCA with accident management measure and PKL counterpart test

Takeda, Takeshi; Otsu, Iwao

Nuclear Engineering and Technology, 49(5), p.928 - 940, 2017/08

 Times Cited Count:4 Percentile:36.37(Nuclear Science & Technology)

Journal Articles

ROSA/LSTF test on nitrogen gas behavior during reflux cooling in PWR and RELAP5 post-test analysis

Takeda, Takeshi; Otsu, Iwao

Proceedings of 25th International Conference on Nuclear Engineering (ICONE-25) (CD-ROM), 11 Pages, 2017/07

JAEA Reports

Data report of ROSA/LSTF experiment TR-LF-07; Loss-of-feedwater transient with primary feed-and-bleed operation

Takeda, Takeshi

JAEA-Data/Code 2016-004, 59 Pages, 2016/07

JAEA-Data-Code-2016-004.pdf:3.34MB

The TR-LF-07 test simulated a loss-of-feedwater transient in a PWR. A SI signal was generated when steam generator (SG) secondary-side collapsed liquid level decreased to 3 m. Primary depressurization was initiated by fully opening a power-operated relief valve (PORV) of pressurizer (PZR) 30 min after the SI signal. High pressure injection (HPI) system was started in loop with PZR 12 s after the SI signal, while it was initiated in loop without PZR when the primary pressure decreased to 10.7 MPa. The primary and SG secondary pressures were kept almost constant because of cycle opening of the PZR PORV and SG relief valves. The PZR liquid level began to drop steeply following the PORV full opening, which caused liquid level formation at the hot leg. The primary pressure became lower than the SG secondary pressure, which resulted in the actuation of accumulator (ACC) system in both loops. The primary feed-and-bleed operation was effective to core cooling because of no core uncovery.

Journal Articles

Contributions of OECD ROSA & ROSA-2 Projects for thermal-hydraulic code validation

Nakamura, Hideo

Proceedings of Seminar on the Transfer of Competence, Knowledge and Experience gained through CSNI Activities in the Field of Thermal-Hydraulics (THICKET 2016) (CD-ROM), 29 Pages, 2016/06

no abstracts in English

JAEA Reports

Data report of ROSA/LSTF experiment SB-HL-12; 1% Hot leg break LOCA with SG depressurization and gas inflow

Takeda, Takeshi

JAEA-Data/Code 2015-022, 58 Pages, 2016/01

JAEA-Data-Code-2015-022.pdf:3.31MB

The SB-HL-12 test simulated PWR 1% hot leg SBLOCA under assumptions of total failure of HPI system and non-condensable gas (nitrogen gas) inflow. SG depressurization by fully opening relief valves in both SGs as AM action was initiated immediately after maximum fuel rod surface temperature reached 600 K. After AM action due to first core uncovery by core boil-off, the primary pressure decreased, causing core mixture level swell. The fuel rod surface temperature then increased up to 635 K. Second core uncovery by core boil-off took place before LSC induced by steam condensation on ACC coolant injected into cold legs. The core liquid level recovered rapidly after LSC. The fuel rod surface temperature then increased up to 696 K. The pressure difference became larger between the primary and SG secondary sides after nitrogen gas inflow. Third core uncovery by core boil-off occurred during reflux condensation. The maximum fuel rod surface temperature exceeded 908 K.

Journal Articles

ROSA/LSTF tests and RELAP5 posttest analyses for PWR safety system using steam generator secondary-side depressurization against effects of release of nitrogen gas dissolved in accumulator water

Takeda, Takeshi; Onuki, Akira*; Kanamori, Daisuke*; Otsu, Iwao

Science and Technology of Nuclear Installations, 2016, p.7481793_1 - 7481793_15, 2016/00

AA2016-0048.pdf:5.15MB

 Times Cited Count:1 Percentile:10.51(Nuclear Science & Technology)

Journal Articles

ROSA/LSTF experiment on a PWR station blackout transient with accident management measures and RELAP5 analyses

Takeda, Takeshi; Otsu, Iwao

Mechanical Engineering Journal (Internet), 2(5), p.15-00132_1 - 15-00132_15, 2015/10

151 (Records 1-20 displayed on this page)